Suzuk-E 

1987 Suzuki RM125 Conversion - Part 7 ...

March 2009

 


Part#6 was crazy busy with machining blanks into foam and casting them off in an Alum Alloy... This episode takes a slower pace and cleans up several loose ends that were unresolved or required immediate attention. 

To begin with, there are no images or video to cover 2 days of building-up the motor shaft, weld, grind, measure, weld, grind, measure... boring boring stuff. But well worth the effort as the MY1020 output shaft is uniformly 1/2" in diameter and fits the 2 1/2" drive pulley perfectly.

Similarly the Dual Blower assembly was removed as it is near useless.

The bike was slated to be torn-down and painted.

 

But in the course of dis-assembly I found that the front casing had broken where the long bolts that hold the motor together threads into. 

Initially I was concerned that this might be a catastrophic failure, but quickly turned the circumstance to my advantage.

 

 

 

 

 

 

 

 

 

 

 

 

The original bolts were replaced with longer, thinner bolts that could extend out the front and be fastened with nuts.

While the rear casing was drilled out to 3/8th" diameter holes for the bolts, which allowed slightly more rotation of the brush-plate to re-time the motor.

 

 

 

 

 

 

 

 

 

 

 

 

Finally I resolved the poor performance of the belt tensioner by adding a much heavier loop spring shown to the right.

This was recovered from a foot brake assembly off another rolling chassis.

In this config the bike was out for a punishing 30 minute run that verified that the drive train is much improved.

In 1st & 2nd gear there is no slippage of the belt unless the rear brake is applied hard (locking the rear wheel).

While in 5th or 6th gear the belt does start to slip if the throttle is cracked open at a standing start.

 

 

The rest of the tear-down and painting went quite smoothly... Along side of the painting, all bearings were cleaned and lubed prior to re-assembly.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Since the drive train was apart I thought it may as well be painted.

I could have covered the rear of the motor casing but I doubt any significant amount of paint dust could have gotten in, and it has run fine for close to an hour un loaded.

 

 

 

 

 

 

 

 

 

 

 

 

 

The lettering on the gear-box pulley is very legible and is another trick that can be pulled out of the bag on future projects.

 

 

 

 

 

 

 

 

 

 

 

 

 

I'm hoping that this is the last time that I re-assemble the bike as it's getting more complicated as features are added.

A day or two passed as I sat by the window waiting for my NEW Odyssey PC625 cells...

 

 

 

 

 

 

 

 

 

 

 

 

 

The Extreme Battery!!!

Extreme Indeed, I agonized over investing more capital into this bike, but given the specs on what these cells can deliver, I had no doubts about investing in quality.

My rational is that the Existing 17Ahr Portalac's were never designed to deliver bursts of 75 to 100 Amps for upwards of 5 secs at a time, whiles these bad-boys can source over 250Amps for close to 30 secs with no ill-effects.

(That's 7,500Amp/Seconds!!!)

 

 

 

 

Not to mention that these cells can sustain deeper discharges, charge faster (provided you have a charger that can deliver more juice) and operate at colder temperatures.

 

 

 

There are only 2 Brand-New cells which are added to existing PC625's purchased new in 2007.

Agreed, this is a sub-optimal solution, but given the light usage that the original pair has seen, and the fact that they have been stored indoors during the winter and charged regularly they should be fine. 

The charging system is still the Yi-Yun 2.5 Amp 48V semi-intelligent charger, though I intend to balance or equalize the individual batteries with a true AGM smart charger every 4th or 5th charge cycle to track how much disparity there is between the new and old cells.

 

 

 

The above cells were sourced from totalbattery.com a Canadian vendor that is an authorized Odyssey dealer. Luckily for me there is a branch in the next town up from ours and was able to receive the cells in 2 days with free delivery (a significant cost when I was checking prices south of the border in the USA).

 

 

 

 

I thought that I was going to pop an an aneurysm when I found that the new batteries weren't going to fit in the existing Bat-Frame...  

And there was no one to blame as I knew I was supposed to measure and mod the bat-frame before painting, but somehow just forgot...

 

 

 

 

 

 

 

 

 

 

 

 

It took a day to get over my own frustration with myself, and another to resolve the issue.

The retro-fit looks less obvious after the batteries are mounted.

 

 

 

 

 

 

 

 

 

 

 

 

 

With the drive train, batteries and general re-assembly settled, the next job is to step-up the cooling of the motor.

Over the course of several road and trail runs the motor temps were topping 100F as measured in the center of the outer steel magnet casing.

If this were July, I'd be quite pleased, but this is Feb/March and the temps never were above freezing, one day was minus 10C.

To the right is a 120Vac Blower recovered from an old Photo-copier (Gray sheet steel construction).

To the left of it is a cheap 75W AC inverter that will provide 120Vac off the auxiliary 12V battery, the inverter also has a USB charging port of MP3 type devices.

 

 

 

 

 

After some bench testing to be sure that the blower is 100% it was married to the remains of the original blower manifold that mates to the motor.

Same old fiberglass and 1/8" plywood fixtures as before.

 

 

 

 

 

 

 

 

 

 

 

 

With the inlet port covered with a simple grate of sorts I hope that this will be all that's required to flow cool air through the motor.

The seams between the physical blower and the manifold are sealed with a measure of hot-glue and duct-tape.

The completed unit is very sturdy...

Given the presence of 120Vac the bike is relegated to only fair weather riding and trail riding up running river-beds is out.

 

 

 

 

 

 

 

 

 

 

 

There is no amount of description that I could write that would convey the trial and error of numerous mounting schemes required to get the air-stream out of the blower aligned to the air-inlet port on the physical motor.

If the motor peaks out at 120 to 130F on a hot summer's day I think that the internal components should be able to stand that range with a constant flow of cool air.

 

 

 

 

 

 

 

 

The revised drive train has close to 1 hour of road and trail testing with much improved results, and about 45 minutes of continuous No-Load testing in the shop.

The last posting on this project will cover a custom 555 timer-based PWM circuit to drive the LED Head-light directly off 12V, the final wiring of the AC Inverter/Blower combo and the Analog Meter config for both Volts and Amps.

Again my thanks to the numerous folks that have taken an international interest in this project!

 

 

 

 

 

...and about 9 days stuffed into 6 mins and 19 sec...

 

 

 

 

 


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